Cooling Water Flow Redistribution

A MW Kellogg ammonia plant had recurring issues with a cooling water heat exchanger plugging with calcium sulfate scale.  Cooling water flowed through the shell side of the heat exchanger.  The process inlet temperature to the exchanger averaged about 350° F. This hot process condition caused the cooling water to “boil” on the tube surface, thus tenacious deposits were left that could not be removed.  The bundle had to be replaced every few years.

Chemtech applied it’s Cooling Water Equipment Reliability Program to the situation.  Flow and temperature surveys showed that the velocity through the exchanger was less than 2.0 feet per second, and the resulting tube wall skin temperature was over 230° F.  Through engineering design, the inlet cooling water piping configuration was altered to allow for cooler first-pass water to reach the exchanger.  Increased cooling water line sizing was installed allowing for additional flow to be achieved and velocities to be increased.  Also, the exchanger baffle spacing was redesigned to increase velocities through the bundle.

The improvements to the system eliminated the deposition in the heat exchanger, resulting in a cleaner bundle, improved efficiency, and longer run-time of the unit.

 

Steam Drum Carryover

A large industrial facility had recurring problems with water droplet carryover in its 1550 psig boiler system.  The carryover resulted in solid deposits in the turbines and loss of turbine efficiency.  It was estimated that the loss of efficiency was costing the plant about 25,000 pounds per hour of steam.

Chemtech provided engineering services and proposed changes to the Chemical feed systems and operation of the steam drum.  It was determined that the previous chemical and operational program was causing foaming in the steam drum.

Once Chemtech’s chemical and operational program was adopted, the carryover was eliminated.  Turbine efficiency remained constant throughout a 3-year run. 

The engineering study followed by the improved system modifications resulted in annualized savings of about $1.25 million.

 

Plant Startup after Hurricane Katrina

A large refinery was affected by the damaging winds from Hurricane Katrina.  The winds damaged the structure and tore several of the shrouds from the top of the tower.  The plant personnel wanted to resume operation as soon as possible, but were unsure how to cope with the loss of the cooling tower, a critical part of the operation.  Chemtech worked with the process engineers at the plant to establish a path forward.

Because Chemtech had operational data on the cooling tower, engineering was able to determine the amount of heat duty each cooling tower cell could perform.  Based on this information, the plant was able to decide which cells to repair in what order to start up individual units in a fashioned sequence.  The plant units were started up in a systematic order corresponding with the cooling tower cells.

The plant personnel estimated that this work allowed several refinery units to be started two days earlier than was originally proposed, resulting in a gain of about $6 million.